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Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools

Received: 12 February 2021    Accepted: 26 February 2021    Published: 26 April 2021
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Abstract

To look at the current arrangement of a creation line in a shop floor of controlling stuff box fabricating industry also, to improve the profitability utilizing lean strategy absent really any influencing current working frameworks. Technique/ Examination: Broad scopes of lean assembling devices are accessible to deal with a wide range of issues looked by changed fabricating businesses. It likewise helps for effective expense decrease of the assembling part and to guarantee the nature of maker and client. Discoveries: The basic Non-Value added Activities (NVA) were perceived and probabilities needed for improvement has been perceived. Value Stream Mapping (VSM) has the standing of finding squander during assembling and business measure which encourage distinguishing and eliminating or stream the worth added steps furthermore, to kill the non-esteem added steps. Application/Improvements: After achievement of fitting lean instruments, it was discovered that the all out arrangement time was consolidated by around 180 minutes and process duration was dense by about 98 minutes which eventually decreases the lead time and builds the efficiency. A lean manufacturing initiative focuses on cost reduction and increases in turnover by systematically and continuously eliminating non-value-added activities. In today's competitive market, lean is turning out to be "the solution" to manufacturing industries across the spectrum for survival and success.

Published in Industrial Engineering (Volume 5, Issue 1)
DOI 10.11648/j.ie.20210501.11
Page(s) 1-6
Creative Commons

This is an Open Access article, distributed under the terms of the Creative Commons Attribution 4.0 International License (http://creativecommons.org/licenses/by/4.0/), which permits unrestricted use, distribution and reproduction in any medium or format, provided the original work is properly cited.

Copyright

Copyright © The Author(s), 2024. Published by Science Publishing Group

Keywords

Lean Manufacturing Tools, Productivity Enhancement, Gear Box, Lead Time, Line Balancing, VSM, Work Standardization

References
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Cite This Article
  • APA Style

    Sivaraman Parthasarathi, Prabhu M. K., Krishanamani J., Mitun L., Prakash Vellingiri G., et al. (2021). Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools. Industrial Engineering, 5(1), 1-6. https://doi.org/10.11648/j.ie.20210501.11

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    ACS Style

    Sivaraman Parthasarathi; Prabhu M. K.; Krishanamani J.; Mitun L.; Prakash Vellingiri G., et al. Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools. Ind. Eng. 2021, 5(1), 1-6. doi: 10.11648/j.ie.20210501.11

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    AMA Style

    Sivaraman Parthasarathi, Prabhu M. K., Krishanamani J., Mitun L., Prakash Vellingiri G., et al. Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools. Ind Eng. 2021;5(1):1-6. doi: 10.11648/j.ie.20210501.11

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  • @article{10.11648/j.ie.20210501.11,
      author = {Sivaraman Parthasarathi and Prabhu M. K. and Krishanamani J. and Mitun L. and Prakash Vellingiri G. and Rahul C. S.},
      title = {Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools},
      journal = {Industrial Engineering},
      volume = {5},
      number = {1},
      pages = {1-6},
      doi = {10.11648/j.ie.20210501.11},
      url = {https://doi.org/10.11648/j.ie.20210501.11},
      eprint = {https://article.sciencepublishinggroup.com/pdf/10.11648.j.ie.20210501.11},
      abstract = {To look at the current arrangement of a creation line in a shop floor of controlling stuff box fabricating industry also, to improve the profitability utilizing lean strategy absent really any influencing current working frameworks. Technique/ Examination: Broad scopes of lean assembling devices are accessible to deal with a wide range of issues looked by changed fabricating businesses. It likewise helps for effective expense decrease of the assembling part and to guarantee the nature of maker and client. Discoveries: The basic Non-Value added Activities (NVA) were perceived and probabilities needed for improvement has been perceived. Value Stream Mapping (VSM) has the standing of finding squander during assembling and business measure which encourage distinguishing and eliminating or stream the worth added steps furthermore, to kill the non-esteem added steps. Application/Improvements: After achievement of fitting lean instruments, it was discovered that the all out arrangement time was consolidated by around 180 minutes and process duration was dense by about 98 minutes which eventually decreases the lead time and builds the efficiency. A lean manufacturing initiative focuses on cost reduction and increases in turnover by systematically and continuously eliminating non-value-added activities. In today's competitive market, lean is turning out to be "the solution" to manufacturing industries across the spectrum for survival and success.},
     year = {2021}
    }
    

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    T1  - Productivity Improvement and Reduction of Lead Time in Manufacturing Industry Using Lean Tools
    AU  - Sivaraman Parthasarathi
    AU  - Prabhu M. K.
    AU  - Krishanamani J.
    AU  - Mitun L.
    AU  - Prakash Vellingiri G.
    AU  - Rahul C. S.
    Y1  - 2021/04/26
    PY  - 2021
    N1  - https://doi.org/10.11648/j.ie.20210501.11
    DO  - 10.11648/j.ie.20210501.11
    T2  - Industrial Engineering
    JF  - Industrial Engineering
    JO  - Industrial Engineering
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    PB  - Science Publishing Group
    SN  - 2640-1118
    UR  - https://doi.org/10.11648/j.ie.20210501.11
    AB  - To look at the current arrangement of a creation line in a shop floor of controlling stuff box fabricating industry also, to improve the profitability utilizing lean strategy absent really any influencing current working frameworks. Technique/ Examination: Broad scopes of lean assembling devices are accessible to deal with a wide range of issues looked by changed fabricating businesses. It likewise helps for effective expense decrease of the assembling part and to guarantee the nature of maker and client. Discoveries: The basic Non-Value added Activities (NVA) were perceived and probabilities needed for improvement has been perceived. Value Stream Mapping (VSM) has the standing of finding squander during assembling and business measure which encourage distinguishing and eliminating or stream the worth added steps furthermore, to kill the non-esteem added steps. Application/Improvements: After achievement of fitting lean instruments, it was discovered that the all out arrangement time was consolidated by around 180 minutes and process duration was dense by about 98 minutes which eventually decreases the lead time and builds the efficiency. A lean manufacturing initiative focuses on cost reduction and increases in turnover by systematically and continuously eliminating non-value-added activities. In today's competitive market, lean is turning out to be "the solution" to manufacturing industries across the spectrum for survival and success.
    VL  - 5
    IS  - 1
    ER  - 

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Author Information
  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

  • Mechanical Engineering, Sri Krishna College of Technology, Coimbatore, India

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